The 72B Mini Project - Changing 72B Speedo

esd3104 Simon Dix
Simon Dix usa  
O'Fallon MO, USA

Total Posts: 59 Latest Post: 2011-12-18 19:35:32
Follow new posts by subscribing to the   RSS Feed
Link to this journal: http://www.mgexperience.net/journal/esd3104






Page :     1   .   2   .   3   .   4   .   5   .   6   .   7      Next →      [10]



Changing 72B Speedo

Simon Dix usa — Posted on The MG Experience
Sunday December 18, 2011 7:35 PM
Just keeping track of the mileage due to a speedo swap.

Removing speedo reading 51,443 and replacing with 50,541


New on the left old on the right

New on the left, old on the right

New on the left old on the right

New on the left, old on the right




. You can hide this ad & support this site by upgrading to a Gold Membership ~ click here for more info.


Comments on "Journal Entry: Changing 72B Speedo" – No comments yet, you can be the FIRST!

You need a Member Account to access this feature. Please sign in or register to post a comment or leave a rating.

 



77B Compression Test Results

Simon Dix usa — Posted on The MG Experience
Wednesday June 22, 2011 7:19 PM
June 22, 2011 - Compression Test relative to slight head gasket weeping above engine number plate.

Run 1 Before Retorque: #1=138, #2=125, #3=138, #4=140

After Retorque Run 2: #1=135, #2=132, #3=138, #4=140

Both tests done with throttle wide open.



Comments on "Journal Entry: 77B Compression Test Results" – No comments yet, you can be the FIRST!

You need a Member Account to access this feature. Please sign in or register to post a comment or leave a rating.

 



Fixing Oil Scraper Ring - 46,198

Simon Dix usa — Posted on The MG Experience
Monday June 21, 2010 10:50 AM
Just to log that the mileage at the time I fixed the #4 piston oil scraper ring was 46,192 on the speedo.



Comments on "Journal Entry: Fixing Oil Scraper Ring - 46,198" – No comments yet, you can be the FIRST!

You need a Member Account to access this feature. Please sign in or register to post a comment or leave a rating.

 



Engine Rebuild

Simon Dix usa — Posted on The MG Experience
Tuesday May 25, 2010 11:02 AM
Just to remind myself the engine rebuild went in at 43,886 reading on the speedo I switched over to for the 1000 TPM OD.



Comments on "Journal Entry: Engine Rebuild" – No comments yet, you can be the FIRST!

You need a Member Account to access this feature. Please sign in or register to post a comment or leave a rating.

 



Compression Test Results

Simon Dix usa — Posted on The MG Experience
Sunday August 10, 2008 10:40 AM
Scarlett readings:
Compression Test Dry
#1 145
#2 160
#3 160
#4 160

Compression Test Wet
#1 165
#2 190
#3 185
#4 190

Subsequent Cam/Intake Exhaust Port Tests in .001's

Ex #1 148
In #2 265
In #3 255
Ex #4 260
Ex #5 194
In #6 239
In #7 265
Ex #8 260

While I was at it dry compression on Tigger was

#1 130
#2 130
#3 128
#4 130


Concern after Valve Adj 1 Not Compressing valve

Concern after Valve Adj - #1 Not Compressing valve Spring

Other for comparision cam issue probably

Other for comparision - cam issue? probably




. You can hide this ad & support this site by upgrading to a Gold Membership ~ click here for more info.


Comments on "Journal Entry: Compression Test Results" – No comments yet, you can be the FIRST!

You need a Member Account to access this feature. Please sign in or register to post a comment or leave a rating.

 



OK so I needed to clean up the console wiring and so I routed the hazard light harness and cigarette harness through the lower hole in the metal frame of the console on the drivers’ side. I wasn’t sure how everything would connect up but it all seemed to work. So, despite the many other things that need doing, I decided to install my stereo.

Having reviewed the wiring diagram I planned to connect the permanent power lead to the purple wiring, the switched power to the green/pink and ground to one of the ground connectors. Using the connectors for the stereo means I need to rethink the wiring of the console light but that will take some more thinking. I wanted to check the stereo out as I bought it a while back and hadn’t even plugged it in.

I used wires from my old wiring harness to match the wires I planned to connect to so that gave me the bullet connectors I would need and I used male & female connectors to join the stereo wires to the wire from the old harness. I did a quick trial run and everything worked, as soon as I remembered to turn on the ignition key, Doh! Since this worked I started to install the holding bracket and found that the hole was about 1/8th inch too small. So I opened it up a little with a Stanley knife and that worked nicely and the bracket fit. After some adjusting of wires I got the stereo to fully sit back into the bracket. It’s a tight fit and the back of the unit presses a little on the heater hoses but nothing too terrible.

Then I did some wire clean up and connected up the 6x9 speakers that I had installed into my speaker boxes and finally got to test the sounds. Sweet! A little more wire tidying up and that will do for the day.


Got some tunes installed and operational There

Got some tunes installed and operational. There’s a rats nest of wires behind there but it works.




Comments on "Journal Entry: More Centre Console – Stereo Installation Done (Mostly)" – No comments yet, you can be the FIRST!

You need a Member Account to access this feature. Please sign in or register to post a comment or leave a rating.

 

Page :     1   .   2   .   3   .   4   .   5   .   6   .   7      Next →      [10]

Join Us Today!

Not a member yet? Sign up now for your FREE Membership account
Members Sign In:



Tip: You can sign in to any AutoShrine website with the same ID and password.

MGExp Menu

Front Page

Membership

Forums

Live Chat

Calendar

Library

Journals

Top Journals

Latest Posts

Browse All

Random Post

Registry

Cars For Sale

Model Pages

Motorsport

Directory

Clubs

Store

Search

Promote YOUR Business or Product on this Website!
Advertising Info

From Your Smartphone
mgexp.mobi

Adjust Text Size

Larger Smaller
Reset Save